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busted piston rod Question

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Old 04-25-2021, 11:14 PM
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Question busted piston rod Question

If I remove the fuel injector and spark plug from broken piston on my 04 TL. Is it likely Ill be able to get 5 miles to my garage?






Will the computer shut it down? Any thoughts would be appreciated.
Old 04-25-2021, 11:40 PM
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Holy shit!

It might still make it 5 miles. Give it a try and report back.
Old 04-26-2021, 12:04 AM
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Okay will do. Topography isn't much uphill. Ill give it breaks also. Assuming it doesn't sound like shit and over heat.
Old 04-26-2021, 12:06 AM
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If you don't hear back that means life turned to a number 2
Old 04-26-2021, 12:11 AM
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"Kids! You can do anything you set your mind to! Run it up on the highway!"

- Key & Peele
Old 04-26-2021, 08:57 AM
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PPiPiP

Originally Posted by Acura TL Builder
"Kids! You can do anything you set your mind to! Run it up on the highway!"

- Key & Peele
Oil pan cover off looks to be piston 3.

Old 04-26-2021, 10:38 PM
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did ya put the pan back on and give it some oil?
Old 04-26-2021, 10:49 PM
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He put the old oil back in to save a buck and afford the new piston.
Old 04-27-2021, 01:54 PM
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I put in 4 n 1/2 quarts

4 full synthetic. New oil pan new oil filter. Removed spark plug lead valve 6 and piston 6 fuel injector lead. About to get a jump from triple A. Would pop start it but I don't know if I should in this condition.
Old 04-27-2021, 02:00 PM
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Another pic of the pan cover off or bottom engine cover what ever it's called? Didn't put it back on cause it was reckt. Ordering a new one and piston today.
Old 04-27-2021, 02:04 PM
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Another pic of the pan cover off or bottom engine cover what ever it's called? Didn't put it back on cause it was reckt. Ordering a new one and piston today.
Also flushed 2 quarts thru it to try to grab any metal pieces
Old 04-27-2021, 02:09 PM
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Old 04-27-2021, 05:07 PM
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Wouldn't idle for long

AAA thought it was a bad alternator(low power output). It was shaking very loud and the alarm wouldn't go off. Had it towed to my St and ordered the piston.

Does anyone think the Alternator has gone bad or is that from the missing piston(spark plug/ fuel injector lead)?
Old 04-27-2021, 06:34 PM
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Originally Posted by Hashezy
4 full synthetic. New oil pan new oil filter. Removed spark plug lead valve 6 and piston 6 fuel injector lead. About to get a jump from triple A. Would pop start it but I don't know if I should in this condition.
So you’ve been in the car for two days now? Do you keep a poop bucket in the truck?
Old 04-27-2021, 06:35 PM
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Yes alternator is bad in this case. Is there any water in your head/tail lights?
Old 04-27-2021, 07:21 PM
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new piston won't do anything if the block is trashed from the piston denting the bore or the con rod putting in gouges. Cams could have damage from all the bits flowing through the oil system. Did the filter have flakes in it? It's prob going to be easier to get a used engine if there is damage to the bore.
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Old 04-27-2021, 07:50 PM
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I thinks its 😎.
Some knicks

No punctures.
Old 04-27-2021, 08:54 PM
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Csmeance is correct. Junk that engine and buy a used one.

But really, how the blinker fluid level?
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Old 04-27-2021, 09:11 PM
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Ill put a vid up on the old

Futube for shits n giggles and ooy awa. The engine was nice the cars a piece of. I think the last owner was a hobo who moved a body. Got it from a hobbit. I'm not quite ready to part with hot betty.
Old 04-28-2021, 08:45 AM
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Wonder when Majofo will return for post his last two messages?
Old 04-28-2021, 01:57 PM
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Busted piston, or busted member?
Old 04-28-2021, 03:24 PM
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Throw that entire engine away. The block is trash and if you ran oil to those heads, metal shavings are likely there. Tow the thing to a shop and find a junk yard engine.
Old 04-28-2021, 09:34 PM
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New piston?...Should run like a clock...
Old 04-28-2021, 09:44 PM
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Is that a rushkin clock emoji? @Pair of TLs It says "Ky-Ky" which is the russian way to spell "Koo-Koo".
Old 04-29-2021, 11:52 AM
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save the oil
Old 05-05-2021, 07:51 PM
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Rounded head bolt 2. Ran a reverse star pattern on the bitch got the other 7 bolts 1/10 of a fuckn turn. Then up comes bolt number 1 wouldn't fuckn turn, so I turned 234 tighty(maybe I really didn't notice shit but I applied good pressure probably like 135ft pounds). then after some struggle I got bolt one 1/5 a turn. went back for 2 and no go. was able to crack the rest loose. Probably get a chisel out or a power drill with a drill bit. Ill probably tighten all the bolts back up before hand. It's a Chinese finger trap with the pressure.
Old 05-06-2021, 08:03 AM
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Break out the fire hammer.
Old 05-09-2021, 10:15 AM
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Just curious, what do you think caused this? These “J” series engines are pretty tough... Hydrolock?
Old 05-09-2021, 07:27 PM
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short answer dick

Originally Posted by TL-Rocket
Just curious, what do you think caused this? These “J” series engines are pretty tough... Hydrolock?
Poor maintenance. The car had been sitting long. Wrong oil old oil non premium gas( I suspect ). I'll have a better idea once this heads off.
Old 05-09-2021, 07:54 PM
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Originally Posted by Hashezy
Poor maintenance. The car had been sitting long. Wrong oil old oil non premium gas( I suspect ). I'll have a better idea once this heads off.
The lower grade fuel was most likely not a contributing factor; some folks here have over 100,000 miles on their 3G TLs with nothing but Regular grade gasoline.
Old 05-10-2021, 08:38 AM
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Got Bolt 2 out

I got 12pt replacements to tighten it back up. The 6pts had all started to warp and I didn't want to chance not being able to get them out. Special thanks to Harbor Freight for having the bolt out sockets that work. Some suggestions don't let your grip slip. sockets round quickly replace them all the time and try to get reinforced metal. I didn't know when starting this project these bolt heads aren't suppose to go in twice.

Old 05-10-2021, 08:53 AM
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Originally Posted by Hashezy
I got 12pt replacements to tighten it back up. The 6pts had all started to warp and I didn't want to chance not being able to get them out. Special thanks to Harbor Freight for having the bolt out sockets that work. Some suggestions don't let your grip slip. sockets round quickly replace them all the time and try to get reinforced metal. I didn't know when starting this project these bolt heads aren't suppose to go in twice.

Rocker arm bolts can go in multiple times. Head studs are one time use.
Old 05-10-2021, 05:18 PM
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that valve train is nasty! Looks like lack of oil changes and other poor maintenance
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Old 05-10-2021, 09:23 PM
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Originally Posted by csmeance
that valve train is nasty! Looks like lack of oil changes and other poor maintenance
Good going Hashezy.
Old 05-19-2021, 05:09 PM
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You get that ram jam piston issue fixed yet?
Old 05-19-2021, 07:32 PM
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Originally Posted by horseshoez
The lower grade fuel was most likely not a contributing factor; some folks here have over 100,000 miles on their 3G TLs with nothing but Regular grade gasoline.
If they're running regular, it's likely they won't make it to 200K. Those clowns who think they're being smart running Regular thinking they're outsmarting the car's computer are bucking for shorter engine life. In 342K miles, only once did the dumb ass attendant put in regular after I told him V-Power 3 times. That's the problem here in NJ, STILL the only state that requires attendants to pump your gas.
.
.

Last edited by DMZ; 05-19-2021 at 07:40 PM.
Old 05-19-2021, 08:18 PM
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Originally Posted by DMZ
If they're running regular, it's likely they won't make it to 200K. Those clowns who think they're being smart running Regular thinking they're outsmarting the car's computer are bucking for shorter engine life. In 342K miles, only once did the dumb ass attendant put in regular after I told him V-Power 3 times. That's the problem here in NJ, STILL the only state that requires attendants to pump your gas.
.
.
Oregon aswell, its annoying, particularly when its a busy station.
Old 05-19-2021, 11:35 PM
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Originally Posted by DMZ
If they're running regular, it's likely they won't make it to 200K. Those clowns who think they're being smart running Regular thinking they're outsmarting the car's computer are bucking for shorter engine life. In 342K miles, only once did the dumb ass attendant put in regular after I told him V-Power 3 times. That's the problem here in NJ, STILL the only state that requires attendants to pump your gas.
.
.
Pump jockeys is so 1950s...good to see Joisey keeping traditions alive.

Oregon, too??

Last edited by Pair of TLs; 05-19-2021 at 11:37 PM. Reason: EDIT: OREGON, too?
Old 05-20-2021, 08:32 AM
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Originally Posted by Pair of TLs
Pump jockeys is so 1950s...good to see Joisey keeping traditions alive.

Oregon, too??
Seems they passed legislation 3 years ago to stop that, and we didn’t see them for 8 months, then suddenly they began coming
to our pumpholes again.

Oregon(Portland) is weird, don’t move here if you can help it.
Old 05-30-2021, 07:14 PM
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Not sure whats wrong now. I had removed fuel pump fuse and the fuel relay. When I push on the gas it isn't feeding. Won't hold an idle and sounds awful. the fuel rail is kind of loose. The front knock sensor broke. I haven't added coolant yet. And I also forgot piston rod bearings on piston 6. Also the front fuel line to fuel rail connector is missing the green fast clip but is fully pressed on. Help!
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